husqyman
Husqvarna
AA Class
This is just to Hi to everyone on Cafe Husky, it is a bit late I Know but many thanks to Xanadu for his wiring diagrams. I am new to Husky ownership but i still remember when I was 19 with a YZ125 (mid to late seventies) and I saw a red & chrome husky on a dealers stand at a meeting in Wiltshire and I thought "one day" anyway back to present I have recently aquired an 1988 430XC that has 18" akront rims fitted front and rear with Bridgestone BT45 road tires fitted all taxwd and M.O.T'd for UK road use and a 1987 250WR that was bought as a non runner to get back to life.
some things I would like some help on if anyone can help. The 430 runs fine but wouldnt clear its throat (4 stroking) I started at the back the gearing had been a bit optomistic for road use with a 16F & 28R it just woudlnt pull that gearing I set it back to standard 13/52? it was better but still 4stroked as the throttle was opened but then pulled my arms off, I fitted a new air filter & cleaned the carb still the same, the needle was on the 2nd from top notch & the pilot screw was only half a turn out, I have moved the needle to the middle notch and with the engine up to temp set the pilot air screw to about 1.5 to 2 turns out it picks up cleanly with no load but I have been unable to check it out due to a bad attack of gout in my right knee which has left me unable to bend it for a week or so. Am I heading in the right direction? I only really want to change one thing at a time to find this problem. thanks for taking the time to read this
some things I would like some help on if anyone can help. The 430 runs fine but wouldnt clear its throat (4 stroking) I started at the back the gearing had been a bit optomistic for road use with a 16F & 28R it just woudlnt pull that gearing I set it back to standard 13/52? it was better but still 4stroked as the throttle was opened but then pulled my arms off, I fitted a new air filter & cleaned the carb still the same, the needle was on the 2nd from top notch & the pilot screw was only half a turn out, I have moved the needle to the middle notch and with the engine up to temp set the pilot air screw to about 1.5 to 2 turns out it picks up cleanly with no load but I have been unable to check it out due to a bad attack of gout in my right knee which has left me unable to bend it for a week or so. Am I heading in the right direction? I only really want to change one thing at a time to find this problem. thanks for taking the time to read this