shawbagga
Husqvarna
Pro Class
			
		seized my 165 yesterday. after an hour of driving got 2 minutes down the road & she locked up. knew straight away so clutched it & rolled to a stop. piston had 32 hours on it so not too bad I guess. leaned rod off too much, ran too hot at cruising speed & game over. spark plug was white! sensitive these lectrons.
 after an hour of driving got 2 minutes down the road & she locked up. knew straight away so clutched it & rolled to a stop. piston had 32 hours on it so not too bad I guess. leaned rod off too much, ran too hot at cruising speed & game over. spark plug was white! sensitive these lectrons. 
 
thought it felt a little underpowered but assumed it was cos ive been riding 300 lately
 but assumed it was cos ive been riding 300 lately . anyway ripped it apart last night(learnt to do a 2T top end in quick time!) & cylinder looks pretty good just gotta clean some piston residue off it. no scratches to lining from what I can see/feel so new slug & shel be good to go again. base gasket didn't even rip apart so just whacked new 125 top end back on & she fired first kick this morning(after putting rod back to where it was).
. anyway ripped it apart last night(learnt to do a 2T top end in quick time!) & cylinder looks pretty good just gotta clean some piston residue off it. no scratches to lining from what I can see/feel so new slug & shel be good to go again. base gasket didn't even rip apart so just whacked new 125 top end back on & she fired first kick this morning(after putting rod back to where it was).
 
never seized a 2T before & kicking myself for fiddling too much, shoulda left well enough alone! what shits me the most is I drove for 2 hours & missed a good ride! ah well lesson learnt. BTW ms3 rod at 50mm was no good, 49mm seems about the best/safest
				
			 after an hour of driving got 2 minutes down the road & she locked up. knew straight away so clutched it & rolled to a stop. piston had 32 hours on it so not too bad I guess. leaned rod off too much, ran too hot at cruising speed & game over. spark plug was white! sensitive these lectrons.
 after an hour of driving got 2 minutes down the road & she locked up. knew straight away so clutched it & rolled to a stop. piston had 32 hours on it so not too bad I guess. leaned rod off too much, ran too hot at cruising speed & game over. spark plug was white! sensitive these lectrons. 
thought it felt a little underpowered
 but assumed it was cos ive been riding 300 lately
 but assumed it was cos ive been riding 300 lately . anyway ripped it apart last night(learnt to do a 2T top end in quick time!) & cylinder looks pretty good just gotta clean some piston residue off it. no scratches to lining from what I can see/feel so new slug & shel be good to go again. base gasket didn't even rip apart so just whacked new 125 top end back on & she fired first kick this morning(after putting rod back to where it was).
. anyway ripped it apart last night(learnt to do a 2T top end in quick time!) & cylinder looks pretty good just gotta clean some piston residue off it. no scratches to lining from what I can see/feel so new slug & shel be good to go again. base gasket didn't even rip apart so just whacked new 125 top end back on & she fired first kick this morning(after putting rod back to where it was).never seized a 2T before & kicking myself for fiddling too much, shoulda left well enough alone! what shits me the most is I drove for 2 hours & missed a good ride! ah well lesson learnt. BTW ms3 rod at 50mm was no good, 49mm seems about the best/safest

 
	 
 
		 
 
		 I gotta learn to leave well enough alone
  I gotta learn to leave well enough alone 
 
		
 
 
		 
 
		 ) & noticed the seal still in that cylinder, thought hey I don't remember the 125 cylinder having one of those, pulled pipe & PV cover & yep-im an idiot!
) & noticed the seal still in that cylinder, thought hey I don't remember the 125 cylinder having one of those, pulled pipe & PV cover & yep-im an idiot!
 
 
		 
 
		 
 
		