As you all know, Coffee (Dean) passed away a couple of years ago. I am Dean's ex-wife's husband and happen to have spent my career in tech. Over the years, I occasionally helped Dean with various tech issues.
When he passed, I worked with his kids to gather the necessary credentials to keep this site running. Since then (and for however long they worked with Coffee), Woodschick and Dirtdame have been maintaining the site and covering the costs. Without their hard work and financial support, CafeHusky would have been lost.
Over the past couple of weeks, I’ve been working to migrate the site to a free cloud compute instance so that Woodschick and Dirtdame no longer have to fund it. At the same time, I’ve updated the site to a current version of XenForo (the discussion software it runs on). The previous version was outdated and no longer supported.
Unfortunately, the new software version doesn’t support importing the old site’s styles, so for now, you’ll see the XenForo default style. This may change over time.
Coffee didn’t document the work he did on the site, so I’ve been digging through the old setup to understand how everything was running. There may still be things I’ve missed. One known issue is that email functionality is not yet working on the new site, but I hope to resolve this over time.
Thanks for your patience and support!
My 2015 TE300 was very rich. Long story short, I am running the N3CH needle (3rd), 35PJ, 168MJ, AS 1.5 turns out and its pretty good now. I'm still not happy with it though, but getting closer. Still have a slew of needles to try yet. I'm at sea level (0-1000), days are probably averaging 14C. I may do a few test runs with the airbox cover removed as this new airbox seems to be restrictive. Down low, the power is good, but mid-top is not great yet. I run the blue PV spring flush.
My adventure continues. After the bike wouldn't start after rejetting with 168 main, 35 pilot, red needle at 3rd position, and clean fuel I decided there is something else going on.
Pulled the exhaust and out came about 6 ounces of fuel. Once it was drained I put the pipe back on and tried again. Still no start but it sounded better. After a bit of cranking I pulled the pipe and it contained more fuel.
It almost sounds like the float is stuck open. Has anyone run into this?
Here's the latest. The dealer returned the bike to stock jetting. Picked up the bike and brought it home. Started it up, and rode it down the road. I slowed down to turn around, and it stalled and didn't want to start. Turned off the gas because I am afraid of it flooding again, and tried opening the throttle slightly. It bogged a little and then started.
Added some fresh fuel, and tried a short loop in my backyard, and it's bogging and loading up down low.
Will call Husky support again, the the dealer and report back.
Seems OK top end wise.
Yes. The dealer checked and reset the float level height. It was also stuck open, which caused the massive flooding.
I called both the dealer and support today and told them the situation. The dealer seems to think this bike doesn't really have any low end and maybe I bought the wrong bike. I don't believe this because I have seen videos posted on you tube of people lugging them around without issue.
Seems like the dealer doesn't really know much about the bike, but I would like to know what others think.
Thanks Cameron. That's why I haven't given up on the bike. I want exactly what you are describing.
What are running for jetting?
Dealer returned my to stock.
Tried removing the side panel a little to allow for more air flow. I didn't notice any difference, and it still loads up and stalls. The reason I think it's too much fuel is because when it does overcome the bog, there is smoke. Otherwise there is almost no smoke at higher throttle.
Probably just going to bring it back to the dealer as its still under warranty. It's basically impossible to ride it as is.