• Hi everyone,

    As you all know, Coffee (Dean) passed away a couple of years ago. I am Dean's ex-wife's husband and happen to have spent my career in tech. Over the years, I occasionally helped Dean with various tech issues.

    When he passed, I worked with his kids to gather the necessary credentials to keep this site running. Since then (and for however long they worked with Coffee), Woodschick and Dirtdame have been maintaining the site and covering the costs. Without their hard work and financial support, CafeHusky would have been lost.

    Over the past couple of weeks, I’ve been working to migrate the site to a free cloud compute instance so that Woodschick and Dirtdame no longer have to fund it. At the same time, I’ve updated the site to a current version of XenForo (the discussion software it runs on). The previous version was outdated and no longer supported.

    Unfortunately, the new software version doesn’t support importing the old site’s styles, so for now, you’ll see the XenForo default style. This may change over time.

    Coffee didn’t document the work he did on the site, so I’ve been digging through the old setup to understand how everything was running. There may still be things I’ve missed. One known issue is that email functionality is not yet working on the new site, but I hope to resolve this over time.

    Thanks for your patience and support!

  • 2 Stroke Husqvarna Motorcycles Made In Austria - About 2014 & Newer
    TE = 2st Enduro & TC = 2st Cross

TE/TC 2015 te300 jetting recommendations

My 2015 TE300 was very rich. Long story short, I am running the N3CH needle (3rd), 35PJ, 168MJ, AS 1.5 turns out and its pretty good now. I'm still not happy with it though, but getting closer. Still have a slew of needles to try yet. I'm at sea level (0-1000), days are probably averaging 14C. I may do a few test runs with the airbox cover removed as this new airbox seems to be restrictive. Down low, the power is good, but mid-top is not great yet. I run the blue PV spring flush.


Switched to:
NEDW (3rd) 38PJ, 172MJ with red spring. Good but a tad rich. I removed the seat and dremel'd off 1/2 of the plastic supporting ribs underneath the seat (on the seat pan). Much better now. Thing is breathing better. My float was also wayyyy out of whack. Set it to 8mm.

Settling on: :banana:
For now I'm running NEDW(4th), 35PJ, 172MJ, AS 2out with red PV spring (flush). Chugging (tight technical) around is good with good transition from low to mid to high. I may change the red spring to yellow however.
 
My adventure continues. After the bike wouldn't start after rejetting with 168 main, 35 pilot, red needle at 3rd position, and clean fuel I decided there is something else going on.

Pulled the exhaust and out came about 6 ounces of fuel. Once it was drained I put the pipe back on and tried again. Still no start but it sounded better. After a bit of cranking I pulled the pipe and it contained more fuel.

It almost sounds like the float is stuck open. Has anyone run into this?
 
Pull your bowl and check your float height at 45degrees. I didn't measure mine but it was wayyy off so I reset to 8.5mm and its alot better now. To make it easier, attach a host to the carb fuel intake and blow into it while you (use finger) move the float up. Then you can tell exactly when the float valve is sealed. Makes setting the float easy and accurate.


My adventure continues. After the bike wouldn't start after rejetting with 168 main, 35 pilot, red needle at 3rd position, and clean fuel I decided there is something else going on.

Pulled the exhaust and out came about 6 ounces of fuel. Once it was drained I put the pipe back on and tried again. Still no start but it sounded better. After a bit of cranking I pulled the pipe and it contained more fuel.

It almost sounds like the float is stuck open. Has anyone run into this?
 
Western Washington
last run at 55 degrees
sea level to about 1500 feet (so far)
Fuel: 32:1 non-ethanol pump gas, 93oct, Amsoil full synthetic pre-mix "Intercepter"
Slide: Stock (#7)
Pilot : 35
Airscrew: 2.5 turns out from full in
Needle: NECJ, 3rd position from the top (RM 250 needle from Rocky Mountain MC/ATV)
Main: 175
Float level: Factory spec checked
Exhaust: Stock pipe and silencer with EE Spark Arrestor end cap

Runs perfect. Lug it around two gears high for any amount of time then snap the throttle and hang on. No bog, no exhaust splooge etc.
Happy - will see what the warmer temps bring.

HR
 
More bad news. After I wasn't getting anywhere with getting the bike to start and it's brand new, I brought in to the dealer in Worcester, MA under warranty.

They called me today and stated the crankcase was filled with fuel and washout had occurred. Work on the bike was stopped while I contact Husqvarna to make my case for warranty work.

It was determined to be a stuck open float which makes sense.

Not real happy with this bike so far.
 
Now I have good news. I contacted Husqvarna US and made my case. They offered to pay around $100 of $150 to fix it. The float level was way off, or stuck from the factory and that appears to be the cause.
 
That sounds like a fluke deal.... and a stuck float couldve been caused by anything..... junk in the gas or something snuck by the air filter....
 
Here's the latest. The dealer returned the bike to stock jetting. Picked up the bike and brought it home. Started it up, and rode it down the road. I slowed down to turn around, and it stalled and didn't want to start. Turned off the gas because I am afraid of it flooding again, and tried opening the throttle slightly. It bogged a little and then started.

Added some fresh fuel, and tried a short loop in my backyard, and it's bogging and loading up down low.

Will call Husky support again, and the dealer and report back.

Seems OK top end wise.
 
Here's the latest. The dealer returned the bike to stock jetting. Picked up the bike and brought it home. Started it up, and rode it down the road. I slowed down to turn around, and it stalled and didn't want to start. Turned off the gas because I am afraid of it flooding again, and tried opening the throttle slightly. It bogged a little and then started.

Added some fresh fuel, and tried a short loop in my backyard, and it's bogging and loading up down low.

Will call Husky support again, the the dealer and report back.

Seems OK top end wise.



Did you or the dealer pull the bowl and check/reset the float height? Mine was off and I've set from 8.5mm down to 7.5mm which seems to be fine now.
 
Yes. The dealer checked and reset the float level height. It was also stuck open, which caused the massive flooding.

I called both the dealer and support today and told them the situation. The dealer seems to think this bike doesn't really have any low end and maybe I bought the wrong bike. I don't believe this because I have seen videos posted on you tube of people lugging them around without issue.

Seems like the dealer doesn't really know much about the bike, but I would like to know what others think.
 
Yes. The dealer checked and reset the float level height. It was also stuck open, which caused the massive flooding.

I called both the dealer and support today and told them the situation. The dealer seems to think this bike doesn't really have any low end and maybe I bought the wrong bike. I don't believe this because I have seen videos posted on you tube of people lugging them around without issue.

Seems like the dealer doesn't really know much about the bike, but I would like to know what others think.


Mine was a bit of a dud until I cut out most of the supporting ribs on the underside of the seat. This allowed more air to get in. Works a lot better now. For kicks, just pull the left side number plate off a little and ride for 5mins. I can lug 3rd, crack the throttle and it'll wheelie.
 
Thanks Cameron. That's why I haven't given up on the bike. I want exactly what you are describing.

What are running for jetting?

Dealer returned my to stock.
 
Thanks Cameron. That's why I haven't given up on the bike. I want exactly what you are describing.

What are running for jetting?

Dealer returned my to stock.



NEDW(4th), 35PJ, 172MJ, AS 2out'ish with yellow PV spring (flush). Chugging (tight technical) around is good with good transition from low to mid to high. I'm at sea level to 1000' and temps still averaging around 14C here on the east coast. I'll try and snap a pic of what I did to my seat to show what I hogged out.
 
Tried removing the side panel a little to allow for more air flow. I didn't notice any difference, and it still loads up and stalls. The reason I think it's too much fuel is because when it does overcome the bog, there is smoke. Otherwise there is almost no smoke at higher throttle.

Probably just going to bring it back to the dealer as its still under warranty. It's basically impossible to ride it as is.
 
Tried removing the side panel a little to allow for more air flow. I didn't notice any difference, and it still loads up and stalls. The reason I think it's too much fuel is because when it does overcome the bog, there is smoke. Otherwise there is almost no smoke at higher throttle.

Probably just going to bring it back to the dealer as its still under warranty. It's basically impossible to ride it as is.



Bummer, let us know how it goes. Interested to hear what the resolution to your issue turns out to be.
 
Brought the bike to Wagner Motorsports and spoke with service. He seemed surprised to see me.

This morning before leaving, I adjusted the air screw out slowly and it seemed to get slightly better the further out it went. I was told you should not have to turn the air screw out more than 2 turns or so, and if you do then pilot jet is too large.

I think it's the pilot jet and the needle. The reason I don't want to change any of it myself is because it's still under warranty.
 
Contacted the dealer yesterday for an update. The bike isn't ready, but I was told they are working with people they know in the riding community to get the bike jetted correctly. I responded that I was pleased they are at least trying something and acknowledged the bike isn't right.
 
After not hearing anything back for several days, I called the dealer for an update. I was told the carb was gone through a few times with no difference. Turns out they found a broken reed, which might be what's causing the problem.
 
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